
- Infrared and Laser Engineering
- Vol. 50, Issue 6, 20210087 (2021)
Abstract
Keywords
0 Introduction
High power laser device requires that laser beam can achieve precision target after long optical path transmission[
Researchers have carried out extensive research and design work about high-stability optical mount. Bullock[
At present, the design and research of high stability optical mount mainly focus on the material selection and matching between the mount and optical parts, as well as the locking mechanism of the adjustability in the mount. However, there are few literatures about the design of the adjustment mechanism which is an important causes for the structure instability of the mounts. In this paper, a novel structure design was put forward aiming at the instability caused by the grease in the adjustment screw structure of the mount. The stability comparison experiment was carried out on the improved structure and the common structure.
1 Mechanical design
1.1 Instability analysis of adjustment structure
Figure 1(a) shows a kind of optical mount structure commonly used in laser system. The mount adopts two adjustment screws with spherical tips (the red circle in Fig.1) and a steel ball to make point contact with the tetrahedron surface, Vee surface and flat surface on the front plate respectively. The totally six point contacts constrain the six degrees of freedom of the front plate and achieve complete degree of freedom constraint. In order to ensure that the front plate is always against the spherical tip and steel ball, two wire springs are used to pull the front plate to the base plate. By driving adjustment screw structure at different position, yaw or pitch position of the optical parts mounted on the front plate can be adjusted. The adjustment screw plays the role of precise driving and maintaining the position stability of optical parts.
Figure 1.A common optical mount used in laser system. (a) Oblique view; (b) Exploded view
The adjustment screw in Fig.2(a) is a common precision displacement driving structure, which consists of a nut and a driving rod. When driving the driving rod, the spherical tip of the rod produces axial micro-displacement through thread pair, thereby achieving precise orientation adjustment of the front plate. The structure is widely used in optical three-dimensional adjustment platform. Designers often use fine thread and limit fitting tolerance to achieve precision adjustment. On the other hand, they always add grease in thread pair to achieve smooth adjustment and repeatability. Due to inevitable straightness machining error of the driving rod and nut and the unsmooth surface of the screw tooth, many partially sealed small spaces are formed on the entire thread mating surface and filled with grease. Under the unidirectional preload of the spring, the grease squeezed on the pressure side of thread mating surface forms hydraulic pressure, leading to a flexible state of non-rigid contact and forming the so-called "piston effect". This phenomenon directly hinders tight fit of the screw tooth surface between the driving rod and the nut (refer to the schematic diagram of the thread pair in Fig.2(b)). This non-rigid contact piston effect is susceptible to environmental micro-vibration and temperature changes, and changes slowly with the creep of grease. Obviously, this slow creep directly causes a slow axial shift of the spherical tips of the driving rod, which in turn causes a slight position shift of the front plate and then changes the precise position of the optical parts.
Figure 2.Cross-sectional view of a common adjustment screw for precision displacement driving. (a) Common adjustment screw; (b) Schematic diagram of the thread pair
Figure 3 illustrates the effect of the axial shift of adjustment screw on the angular position of optical part. Structural deformation caused by stress is not within the scope of this work. Due to micro-vibration and temperature fluctuation, the spherical tip of adjustment screw 1 moves from point B to point B1 and produces a small displacement
Figure 3.Effect of the axial shift of the adjustment screw structure on the position of the optical part. (a) Schematic diagram of optical mount disassembly; (b) Position change of optical part
The coordinates of B1 and C1 points are (0, l, z1+
This work mainly focuses on the change of the angular position of optical parts. According to the normal vectors before and after optical surface change, the cosine angle in the direction of horizontal yaw and vertical pitch are:
Among them,
From equations (2) and (4), we can get
By introducing equations (5)-(6) and (9)-(12) into equations (7)-(8), it can be obtained that:
The unit of z1, z2,
Figure 4.Effect of the axial initial position and axial shift of the adjustment screw on the angle position of the optic part
1.2 Improved design of adjustment screw structure
Some manufacturers may design a grease-free adjustment screw structure by selecting wear-resistant materials and controlling the thread clearance of the thread pair and the roughness of the thread surface to achieve the smoothness and precision of adjustment. However, this kind of structure still wears out after working for a period of time, and the material requirements and processing are relatively strict, and the price is also relatively costly. Furse[
Figure 5 shows an improved adjustment screw structure which process n (n≥3) axial slots on the inner thread surface of the nut. The axial slots are uniformly distributed along the circumference of the thread surface, and its maximum radial depth H is greater than the major diameter radius D/2 of the thread. The width of slot is slightly larger than the minimum machine width of WEDM (electrical discharge wire-cutting). The cross-sectional shape of the slot in this work is U-shaped, and the design parameters are shown in Tab.1. In practical use, the number and size of axial slots should be determined according to the amount of grease that can be filled in the thread pair. The cross-sectional shape is mainly convenient for processing.
Figure 5.An improved adjustment screw structure. (a) Exploded view of the structure; (b) Thread fit; (c) The cross section of
Parameters | Numbers of slots | D/mm | D1/mm | H/mm |
Value | 3-6 | 7 | 6.65 | 0.5 |
Table 1. Design parameters of the axial slots of adjustment screw structure
Under the action of unidirectional preload of the springs, most of grease filled in the mating surfaces of the screw teeth flows into the axial slots for storage. Since the slots run through the entire thread surface, the amount of small space that is partially sealed in thread pair is greatly reduced. This behavior reduces the hydraulic pressure and makes the screw tooth surface rigid contact as well, alleviating the piston effect. Each time the driving rod is adjusted, the screw tooth surface carries grease from the axial slots into the thread pair to realize the lubrication of the adjustment. When the driving is over, most of the grease will quickly flow into the axial slots, and only a small amount of grease is chemically adsorbed on the screw tooth surface. This achieves close fitting of the screw tooth surface and improves the support stability of the optical mount. It should be noted that the axial slot depth should be as small as possible when it is greater than the major diameter of the thread. This is to avoid excessive grease attached to the bottom of the groove, which cannot be carried by the screw tooth surface into the thread pair to play a lubricating role.
2 Experiment
The purpose of the experiment was to verify the effectiveness of the slotted adjustment screw proposed in this paper compared to the un-slotted adjustment screw. Firstly, a test platform was set up to measure the axial micro-displacement of the two adjustment screw structures under the action of unidirectional preload. Secondly, the two adjustment screws were installed on the two optical mounts with same specification, and the structural stability comparison test was carried out. Both tests evaluated the stability change by observing the position changes under several thermal shockings.
2.1 Stability test of adjustment screw structure
Figure 6 is the schematic diagram of two different adjustment structures. The two structures have the same specifications of the driving rod (Fig.6(a)) and the two nuts have the same external dimension and the same specification of thread size. The specific design parameters of slotted nut (Fig.6(b)) refer to Tab.1. The internal thread surface of the un-slotted nut has no axial groove (Fig.6(c)). With reference to the force of the adjustment structure in optical mount, a test device (shown in Fig.7) was built to compare the stability of the two adjustment structures. The device adopted two wire springs to press clamp against one end of the driving rod to achieve unidirectional preload. The other end of the driving rod was pressed against the contact of the micrometer gauge to record the change of the axial clearance in the adjustment screw. The smallest scale of the micrometer gauge is 1 μm. In the test, an adjustable temperature heating lamp (not shown) was installed on the top of the device to carry out thermal shocking. When heating the structures, the heating temperature, heating time and heating direction were kept same to ensure that the temperature changes have the same influence on the micrometer gauge.
Figure 6.Diagram of adjustment screw and nuts. (a) Adjustment screw; (b) Slotted nut; (c) Un-slotted nut
Figure 7.Test of axial micro-displacement of adjustment screw. (a) Top view; (b) Oblique view
After filling with the same amount of grease, the two adjustment screws (the slotted and the un-slotted) were installed in the same way as shown in Fig.7 for the same number of thermal shocking tests. A single thermal shocking was to heat the structure with a maximum temperature of 35-40 ℃ for 1 h, and then record the dial indicator before heating and after cooling. Figure 8 plots the change of micrometer gauge values of the two structures under several thermal shocking tests. In 9 thermal shockings, the axial shift (7.7 μm) of the un-slotted structure was larger than that of the slotted structure (2 μm), and it was still increasing. While the position of the slotted structure tended to be stable.
Figure 8.Tests of axial clearance change of different adjustment screw structures
In the slotted adjustment screw structure, the grease on the squeezed side flows into the axial slots under the action of the unidirectional preload and the screw tooth surface produces a large area of tight fit. In the un-slotted structure, the hydraulic pressure formed by the many partially sealed small spaces hindered the close fit of the screw tooth surface. With the action of the thermal shockings, the grease squeezed in the thread pair was further reduced. Since the internal screw tooth surface had produced large contact, the axial clearance of the slotted structure changed little, and the micrometer gauge changed little too. While in the thermal shocking tests of the un-slotted structure, the grease squeezed in the pressure side gradually flowed into the non-pressure side under the effect of temperature change and unidirectional preload, resulting in a large change in the axial clearance. The results show that the existence of axial slots could improve the stability of adjustment screw structure under unidirectional preload.
2.2 Stability test of optical mount
The effect of two different adjustment screws on the stability of the optical mount was tested. In the experiment, two optical mounts with same specification were installed with the slotted and un-slotted adjustment screw at the same position respectively. It can be seen from the analysis in Section 2.2 that the axial shift of the adjustment screw 1 only affects the pitch position, but has no effect on the yaw position. In order to enhance the contrast, the mounts both installed the adjustment screw at point B, and the rest of the adjustment positions were replaced by stainless steel balls, as shown in Fig.9. The driving rod only affected the pitch position of the optical part.
The current methods of measuring the stability of optical mounts are mainly developed for a single mount. Tapply[
Figure 9.Optical mounts with different adjustment screw structure. (a) The un-slotted; (b) The slotted
Figure 10.Light path diagram for stability comparison[
Figure 11 shows the change of angular position of the two mounts after two consecutive thermal shockings. Before and after the first thermal shocking, a certain amount of angular shift both occurred in the pitch position of the two mounts. After the second thermal shocking, the pitch value of the slotted structure had little change while that of the un-slotted structure still had a certain shift. Within the two thermal shockings, the yaw values of the two mounts both changed little, so they were no longer used as the measurement index for comparison in this paper. In addition, the angular position of the two-dimensional direction (yaw and pitch) of the slotted structure was stable with the change of temperature, and the spot was not disturbed. However, that of the un-slotted structure produced a large disturbance with the change of temperature. This was due to the fact that there was more grease on the pressure side of the thread pair in the un-slotted structure than in the slotted grooved structure. When the temperature changed, the creep of grease squeezed on the pressure side could easily cause the driving rod to be unstable relative to the nut.
Figure 11.Thermal shocking tests of two optical mounts. (a) The slotted; (b) The un-slotted
Several thermal shocking tests were carried out continuously on two optical mounts. For each thermal shocking test, the data one hour before thermal shocking and the data one hour after cooling to room temperature were extracted respectively, and the average value were taken as the angular position before and after each thermal shocking test. Figure 12 plots the change of pitch position of the two mounts in several thermal shocking tests, in which the temperature was the normal temperature value of the corresponding mount after each thermal shocking. After several thermal shocking tests, the environmental temperature deviation of the two mounts didn’t exceed 0.3 ℃. In the 1-4 thermal shocking tests, the angular shift of the un-slotted structure had larger fluctuations than that of the slotted structure. Since the fifth thermal shocking test, the angular shift of the two structures kept the same. Compared with the un-slotted structure, the angular shift of the slotted structure was slightly reduced, but there was still a tendency to continue to increase.
Figure 12.Angular shift of optical mounts under thermal shocking
To quickly achieve stable distribution of the grease and reduce the distribution of grease in the squeezed side of the thread pair, the slotted optical mount was put into the incubator for sufficient time baking. In order to compare the effect of high-temperature baking on the two mounts, the un-slotted structure was also put into the same incubator for the same baking. The baking process was to bake the two mounts for eight hours a day (80 ℃) for several days. The baking temperature must not be higher than the dropping point of the grease. The baking time should be as long as possible. In this experiment, the baking duration in this work was one week, which has achieved the desired effect. The purpose of shutting down and cooling after baking was to achieve a stable state of the grease distribution in the thread fit. Then the two mounts was taken out and the stability comparison test was carried out again. In addition, the experiment added a comparative test between the heat-treated slotted mount and the grease-free mount to compare the effect of heat treatment on the stability of the slotted mount.
The angular position of the heat-treated slotted structure only changed slightly in the first two thermal shocking tests, and maintained a stable state under thermal shocking tests (Fig.13(a)). However, the angular position of the un-slotted structure always changed greatly after each thermal shocking test. The angular position of the grease-free optical mount was always in a stable state under several thermal shocking tests, while that of the heat-treated slotted structure only fluctuated slightly during the 5th-6th thermal shocking test, and then returned to a stable state (Fig.13(b)).
Figure 13.Angular shift of different optical mounts under thermal shocking. (a) The slotted (grease+heat treatment) versus the un-slotted (grease+heat treatment); (b) the slotted (grease +heat treatment) versus the structure (no grease)
Further, it could be seen from Tab.2 that the angular shift of the heat-treated slotted structure in two comparative experiments was only 14-15 μrad, which was close to the angular shift of the grease-free structure (8 μrad), and far less than that of the un-slotted structure (34 μrad). The results show that the stability of the heat-treated slotted structure was close to that of the grease-free structure, and was better than that of the un-slotted structure.
Slotted 1-8 tests | Un-slotted 1-8 tests | No-grease 1-8 tests | |
Angular shift (pitch)/μrad | 14-15 | 34 | 11 |
Table 2. Angular shift of different optical mounts after baking
3 Conclusion
This paper studied and analyzed an instability factor of optical mount in laser system. The effect of the axial shift of the adjustment screw caused by the creep of grease on the position of the optical part was analyzed theoretically. It was concluded that the axial shift of the adjustment screw was an important factor for the position instability of the optical mount. An improved thread adjustment structure was proposed. A number of axial slots evenly distributed in the circumferential direction were machined on the inner thread surface of the nut. The maximum radial depth of the axial slot was larger than the major diameter depth of the thread. The structure combined with heat treatment process greatly improved the stability of optical mount. The experiment tested the change of internal axial clearance of two different adjustment screws (the slotted and the un-slotted) under thermal shocking tests. The results showed that the slotted structure could reach stable quickly under the thermal shockings. Secondly, two optical mounts with same specification were used to install the two adjustment screws to carry out the stability comparison test. The results showed that under several thermal shocking tests, the angular shift of the slotted mount was slightly reduced compared to that of the un-slotted structure, but there was still a tendency to increase. Furthermore, in order to achieve a stable internal grease distribution, a long time high-temperature baking for heat treatment process was carried out on two mounts. The stability comparison experiment was built again, and the stability of the slotted heat-treated mount was compared with that of the un-slotted mount and that of the grease-free mount respectively. The results showed that the stability of the heat-treated structure was close to that of the grease-free, while was better than that of the un-slotted structure. The optical mount with slotted heat-treated adjustment screw combined with baking heat treatment process shows more excellent stability. This adjustment screw structure can be used in the optical mechanisms with high stability requirements.
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